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I seem to have solved this issue, it was a combination of below
Too high controller frequency
Was running at 200hz, the errors went away when brought down to 10hz
Latency Setting not setup according to u2d2 settings
Once the latency was set to 1ms, the max frequency jumped to around 40-50hz
I believe one of the reasons for this is that the read and write functions are called once init fucntion is done, if we can delay till after on activate function, this problems go away at 200hz+ on my system, will put a pr for the same
System Info
humble
ros-humble-dynamixel-workbench*
ros-humble-dynamixel-sdk
I am encountering the following errors in my log
I am however able to control the motor using Dynamixel Wizard 2.0
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